Historical Articles
June, 1953 issue of Plating
SOME EXPERIENCES IN PLATING ON NICKEL
SILVER
George Schore, Technical Sales Representative,
Frederick Gumm Chemical Company,
Kearny, N.J.
INTRODUCTION
In the manufacture of metal pen parts, designers requested the use of nickel
silver, and also specified a bright plated finish for added eye appeal.
It was found that, although a chromium finish was adequate, a brighter
looking
finish
was obtained by using bright nickel plus chromium or bright nickel plus
rhodium. This paper has been written to outline a series of practical
and technical
considerations that were followed in solving difficulties that cropped
up with an especially
troublesome lot of basis metal.
NORMAL PROCEDURE
The firm at which the work was carried out is a fair-sized job shop in
the New York area and had been successfully nickel and chromium plating
nickel-silver
parts for some time. One of its regular production items was a part of
this metal
that was nickel plated, engine turned and finally chromium plated. An
alternate finish on the same item was the use of a nickel plus rhodium
plate followed
by an engine turning operation. Plating on nickel silver was not a new
problem, therefore, to the finishing department of this job shop. The
following is
the
cleaning and plating cycle which was used with good results on such parts.
- Mild type soak cleaner (optional
and used when required)
- Water rinse (optional).
- Electrocleaner.
Cathodic in a mild composition for 30 to 60 seconds at 6 volts and a temperature
of 180° F
- Water rinse
- Anodic etch in 15 per cent (by weight)
sulfuric acid solution at room temperature for 15 to 30 seconds at 6 volts
- Water
rinse
- Proprietary bright nickel plate
at 30 amperes per square foot for 4 to 5 minutes at a pH between 4.0 and
4.5 (colorimetric).
- Water rinse and dry, or
- Proprietary
chromium plate (2 minutes), or
- Rhodium plate (2 minutes) in a sulfate
solution
This cycle was operated successfully
over an extensive run of parts with practically no trouble. It was used on
pen parts (see Fig. 1)
with one
modification, and
that to avoid possible etching of the highly polished finish. The
modification was the substitution of a 5 per cent sulfuric acid immersion
step for
the anodic sulfuric etch. Several thousands of these articles were
successfully processed
using the immersion dip modified cycle outlined above. The customer’s
approval of the plate quality attested to the kind: of performance
effected through use
of the cycle.
REVISED PROCEDURE
When the next: shipment of material came in for plating, difficulties
arose, and the sequence of operations used so successfully above
just did not
give the anticipated results. A more exact description of the part
will give a
better idea of the customer requirements on this deep drawn cap.
It was perfectly smooth,
without any lines or design marks, and the customer specified that
there was
to be no “orange-peel”, pitting or roughness. The caps
were to be covered with chromium over their entire outer surface.
After plating, a
vent
hole was to be pierced into the item. Strict adherence to the specifications
was to be assured by a 100 per cent inspection of all parts.
At
first, when some of the new lot was processed, results looked
favorable. Inspection during the run was provided, as specified,
for coverage
of chromium, peeling,
roughness and color. Inspectors also hammered down each fiftieth
cap and checked for blistering and adhesion as affected by the
test. Through
all
these tests
the results appeared to be all right. Not until the customer
pierced the vent hole into the caps did any sign of trouble show up. A
25 per cent
rejection rate
was found at this step, apparently caused by the ripping of the
plated layer around the vent hole. All the more baffling in this
situation
was that the
remainder, or 75 per cent, of the caps were not affected by the
piercing operation. In an
effort to get top adherence, it was decided to activate the nickel
silver.
Activation Steps
Sulfuric acid solutions in concentrations varying from 5 to 50
per cent were tried with both anodic and cathodic treatments.
These steps
all
helped in
improving the adhesion, but rejects for “orange-peel” or
pin holes increased to such a high point that there was no
over-all improvement in the production
rate. At this point, the thought occurred to the writer, that
perhaps the type of activation used on some of the bright nickel
solutions prior to chromium
plating would be the answer to the problem at hand. The method
of activation using direct
current treatment in a solution of sodium cyanide was thus
attempted. Results were so encouraging on a small run of parts
put through with this technique
that a large production lot was processed. Tests using the
hammering procedure described
above were always excellent so that a 12 per cent rejection
by the customer was completely baffling. Since the rejections
occurred only after the piercing,
no
immediate solution appeared to be available. The possibility
of getting around the problem by piercing initially was promptly
set aside because of the difficulty
of chromium plating around the hole.
Stress Reducing Steps
Fortunately, at this time, Dr. Walter R. Meyer suggested to
the author that the stress in the nickel deposit was greater
than
the bond strength
between
the plated
layer and the basis metal. It was, therefore, decided to
lower the pH of the nickel bath to about 3.0 (colorimetric); adjust
the current
density
to a maximum
value between 10 and 15 amperes per square foot and to lower
the plating time to about 2 minutes. With this final modification
to
the plating
cycle
put into
practice, it was found that the end results were satisfactory
and the problem solved. Rejects were then kept to within
3
per cent
which was
a figure
set as allowable by the customer. The tested and production-proved
cycle for
the troublesome
lot of work is as follows:
- Soak cleaner (mild alkali)
- Water rinse
- Electrocleaner. Cathodic at 6
volts for 15 to 30 seconds in mild alkali
- Water rinse
- Cyanide activation
(16 oz/gal solution of sodium cyanide). Room temperature for 15 to
30 seconds at
6 volts, cathodic.
- Water rinse
- Immersion in 5
per cent (volumetric) sulfuric acid solution for 10 seconds
- Water rinse
- Proprietary bright
nickel plate. At a pH of 3.0 (colorimetric) and 15 amperes per square
foot for
two minutes. Bath
temperature, 130°F ± 5°F
- Water rinse
- Proprietary chromium plate—2
minutes
- Water rinse
- Dry
CONCLUSIONS
Though the treatment cycle immediately
above was found to give acceptable
results in the
plating of nickel
plus chromium
on
an especially troublesome
lot of nickel
silver parts, it by no means will
assure good results
if attention is not paid to other
good plating practices. The water rinsing
steps are
as critical
in the
operation as any of the other ones
and it must be emphasized that
adequate rinsing
in good
clean water
must be observed.
Actually, the entire
cycle could have been
dropped, and with it the numerous
headaches that occurred, had the customer decided
to
go along
with a finish
which was just
a
shade
different. That
finish was one
brought about by the use of a straight
chromium plate without
any underlying layer of bright
nickel. But it is just these variations in
finish requirements
that make the job-shop operation
such a nerve-racking one. It is
hoped that the above-outlined lesson
learned, by
the writer, as to the influence
of
bond strength
in the plating of job lots of metal
parts will be of assistance to
others in the
field, and
it is mainly
for that reason
that this paper
was written.
The
cycles outlined, naturally will
work in the majority
of cases, but it is also apparent
that circumstances may be
such that
results obtained
from
the use of
the sequences will not give maximum
benefits as regards adhesion.